Well I’ve been busy on the LE again and think I may have found the ignition problem.
I needed to know what depth I had between the top of the ignition unit’s top plate and the bore in the end of the crankshaft, this meant taking out the fixing bolt and when doing this I steadied the shaft from turning by holding the unit, as soon as I had eased the centre bolt a little I felt the bob-weights move under my fingers when they had been solid before.
On trying the unit I found the bob-weights would now open out readily. I re-tightened the centre bolt and found they were locked up so that while the engine had been running it had been locked on full retard, no wonder performance had seemed lacking!. It looks like the last person working on the engine electrics had over-tightened the retaining bolt and jammed the unit.
Hopefully the unit has not been damaged by this but we’ll have to see.
I’ve since tried her up the back lane and she seems a bit livelier, but I’ve found that I omitted the seal between the carburetter and the inlet manifold when I put things back together last time. On having a look at the seal it appears to have been cut from a piece of old inner tube, it’s certainly been either knife or scissor cut so I’ll need to get a new one up.
I’ve just totted up what bits I now need, it may be small stuff but it totals out at about 21 quid so It’s worth sending down for them.
It’s amazing how it’s a number of small things are giving the problems now! I had thought that all that was wrong with her was the corroded water pipes! But I suppose that’s what happens when you take on a rebuild.